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31-3-2017 Buell XB12R big inspection
27-4-2017 - What did we do today: 31-3-2017 Buell XB12R some TLC ( aka big inspection ) wheel bearings Dyno, exhaust strap
nice 07 Xb12R for inspection to day
comming in hot.. so drain the plugs right way
removing the covers and loosen the clutch adjuster little dab off neverseas on the threads
gear box drain plug.. a litle debris is ok
plug in and gear box oil back in
chin spoiler has been juttering to the oil filter ( chin spoiler is loose )
fresh filter on hand tight
needed the breaker bar to loose the axle ..
rear brake off
rear wheel in the stand.. 5e gear and checking the primary chain , needed to adjust this one a little
nice wheels... remove the inner belt guards.. so you don't damage
belt check .. ok
rear wheel bearings.. not ok
pressing in the new bearings using stamps and holders
and axle cleaned and lube... back in
front plug change from below
check the plug cables for rubbing
rear plug back in
point the front plug cable in so it douse not run against the cables
as this is a 2007 model.. look extra at the reasr rocker cover.. it has been cleaned.. but are the gaskets replaced.. decision was made to check theme
a i really don't want this exhaust to determinate any furter ( rear is fixed already ) leaving this on and make a engine support with some blocks off wood and a prybar
engine supported.. trying to loosen the front bolt.. the insert is loose.. with a big ratched , and spanner to hold the socket , so you can make a turn to put some load on the bolt.. usualy after a few turns it will pop loose
as it did.. will clean the axle before it goose back in
off course we remove the left foot peg bracket before dropping the engine
better look.. cover off indeed orange "old" gaskets
new black ones in and cover back on
mnnn head temp sensor the terminal is loose.. will repair this
frame insert... to put a socket on i need to remove the bump rubber
tiny plate with rubber bump stopper on
1 inch socket and frame insert out
loctite on and turn it back in
and bump rubber back on
looks like the front has also been leaking,, with the engine down.. no work at all to do this
yep front ones also old style orange
engine back up the loctite had time to dry.. front bolt cleaned and lubed a little... tq to 66 NM
head sensor wire new terminal on
and stack and airbox back on
front end check
wheel bearings.. are starting to get bad .. just replace theme
mnn i see this happen more.. this one also overtighten the axle ... the allen key forces the end off the axle out a little
the axle has become 0.20 thicker at the end where the socket needs to go in
while normaly the axle is 30 mm , this way the axle can become tight in the front leg.. and the fork can not slide in postion
a little skim on the late and the end is back in shape
works better like this :-)
front end out to refesh the oil
protecting the top caps
mnnn right leg.. looks like it is bend a little , almost not visible at the outer leg while mounted.. but directly visible with the rebound damper is out the middle
legs serviced .. tighten the top clamps only
now retighten the steering head bearings
and than the lower clamps
stock R postion
but as this customer is a long guy.. advised hime to go for S pegs .. easy and more leg room
front brake light switch did not work... wonder way ;-)
front brake fuild change
and rear
and rear
light no worky
very hard to get to .. so i removed the light unit.. the ground tab is corroded off .. no wonder ..
with some new connections , the lights work again.. and faring can be put on
contact... mnn missing one light ... oil pressure
mnnn some thing fishy here
the oil line is turned so that it broke the oil pressure switch
ok.. oil filter off again.. to give room for the oil pressure switch
old broken one out and new one in
yes working now... warm up. oil level check and test ride :-)
i see some thing wrong with my front end.. !!! i can see the balls... mnn that is not good please come by
the left side was completly out allready
retreving the inner ring and some loose balls , make it so i gan still use a puller ( or try to )
normaly this works , as it did now.. saves allot off time getting the outer race out
lady with experiance :-) did not expect this on the dial :-)
ready to rumble again
bike off the dyno., front strap broke..
eehh strap did not break . the bolt did .. i think it was to tight .. the expansion when the exhaust gets hot is big
down side you need to loosen the exhaust to replace the strap
other strap on.. put a counter nut on the bolt.. these remus straps have a problem with these bolts runnign loose